That’s exactly what Jack was doing one fine Thursday afternoon in his Cirrus SR22 Turbo. The airplane had been performing flawlessly, so after landing at Elko, Jack was floored to find engine oil dripping out of the left exhaust stack and streaked along the left underside of the fuselage. This is not the sort of thing that you want to see when you’re in the middle of nowhere.
Jack checked with the FBO but its A&P had gone home for the day. He phoned Savvy Aviation’s 24/7 hotline number and spoke to A&P/IA Tony Barrell, one of our most experienced account managers and former director of maintenance at a large Cirrus service center.
Remote diagnosis
Jack sent Tony several smartphone photos of his oil-covered airplane and explained that the airplane had recently come out of an annual inspection during which all its oil hoses had been replaced after 10 years in service. Tony suggested that Jack look closely at the oil lines to see if any appeared to be chafed or have loose connections.
Jack removed the top cowling and sent Tony a half-dozen photos of what he found. There was oil all over the place on the left side of the engine, but all the oil hoses appeared to be secure and intact. One photo caught Tony’s experienced eye, however. Tony passed the photo to another of his Savvy colleagues, Al Hawthorne, an A&P/IA who works closely with a big Cirrus service center near Sacramento, California.
“Check out the valve cover picture that Jack’s sent,” Tony told Al. “Looks to me like the cover is cracked and bulged out. Possibly the bolts securing the rocker shaft came loose. Hope not, but it looks possible. Shop on the field can’t look at this until tomorrow. Can you get a new valve cover overnighted to Elko?”
Al checked with the Sacramento service center and located a valve cover. It was too late to ship the part out that day, so Al arranged for it to be overnighted on Friday, together with a new gasket and locktabs.
Meanwhile, Jack had removed the damaged valve cover and verified that both bolts securing the rocker shaft had backed off despite the safety locktabs. The rocker shaft was loose and the rocker assembly had been banging against the loose bolt heads, causing them to gouge the inside of the valve cover to the point of cracking it and causing it to leak oil.
Seeing how much metal had been gouged from the inside of the valve cover, Jack became concerned that his engine might be contaminated with metal. Tony assured him that there was nothing to worry about because any metal that managed to get out of the valve cover area would have been caught by the suction screen or the oil filter.
There’s no Saturday delivery to Elko, so the new valve cover, gasket, and locktabs arrived on Monday morning. In the meantime, the local A&P at Elko had removed the loose rocker bolts and found that they were badly stripped and stretched and unusable. New bolts had to be overnighted to the FBO.
The new bolts arrived Tuesday morning, and the local A&P installed, torqued, and safetied them; then installed the new valve cover and gasket. The engine compartment and oil-covered fuselage were washed with solvent, and the engine cowling was reinstalled. An extended runup and brief test flight revealed no further oil leaks. Jack was finally able to resume his trip after what turned into a six-day fuel stop in the middle of nowhere.
“We’re back home and she flew great,” Jack reported to Tony and Al. “We’re going to do an oil and filter change tomorrow.”
This was a close call. Had Jack not caught this problem when he did, it wouldn’t have taken long before the valve cover failed to the point of causing engine oil starvation, valve train failure, or both. The fortuitous timing of Jack’s fuel stop in Elko combined with Tony’s experienced eyes saved the day.
That leaves the obvious question: How’d this happen? There’s really only one thing that could have caused it to happen, and that is failure to torque the rocker retention bolts properly before setting the locktabs. These bolts are subject to high repetitive stress, so the integrity of the joint depends pivotally on proper torque (and preload) on the fasteners. If the bolts weren’t installed with the requisite torque, there’s no way the locktabs could survive for very long.
Failure to torque these bolts properly is not the sort of thing that could easily happen at the factory, where fasteners are installed using purpose-made, nonadjustable torque wrenches. Nor would it be likely to happen at an FAA-certified engine repair station, where the technicians are experts at engine assembly. It very likely occurred during cylinder work in the field, where in my experience reassembly errors are disturbingly common.
A case of elusive high CHT
Wade’s Cirrus SR22 was based in Wisconsin where it’s frigid in the winter and hot in the summer. The airplane performed fine in the winter, but in the summer Wade couldn’t keep the number 3 cylinder head temperature under 400 degrees Fahrenheit no matter how hard he tried. The other five cylinders of his turbonormalized Continental IO-550-N seemed well behaved, but cylinder number 3 was simply hot-headed.
Wade had been battling this problem for two years. He’d asked his shop in Wisconsin to fix it. He’d taken it to a Cirrus service center in Minnesota. He’d even taken it to the developer of the Cirrus turbonormalizing supplemental type certificate—Tornado Alley Turbo in Oklahoma—for an annual inspection. Nobody was able to cure the problem.
It wasn’t for lack of trying. These shops had checked the cooling baffles and baffle seals, checked the magneto timing, borescoped the cylinders, replaced the spark plugs, cleaned and tweaked the fuel nozzles, and swapped CHT probes. Nothing seemed to help.
Wade contacted Continental Aerospace Technologies, where the technical representative said they never worry about CHT unless it exceeds 420 degrees F, and pointed out that Continental’s CHT redline is 460 degrees F. Wade remained unconvinced; he believed his number 3 cylinder was unlikely to live long and prosper at such a high CHT.
Wade brought his problem to me and I got my technical director, Jeff Iskierka, involved. We reviewed the aircraft’s digital engine monitor data and studied its maintenance history to see what had been tried and what might have been missed. The various shops that had been working on Wade’s SR22 were telling him that the only thing left to try was to replace the hot-running number 3 cylinder. Wade was willing to try this, but Jeff and I suggested that he hold off.
For one thing, cylinder replacement is sufficiently invasive that we recommend not doing it unless absolutely necessary. Wade’s number 3 cylinder had good compression and looked fine under the borescope. Removing it under these circumstances seemed like a desperation move.
For another, Jeff and I agreed that Wade’s high CHT problem simply did not “feel” like a cylinder defect. Both of us were convinced it was most likely caused by insufficient cooling air passing over the cylinder’s cooling fins, even though several different shops had looked at the cooling baffles and baffle seals and pronounced them healthy.
Given that only one cylinder was running hot, Jeff and I suspected a possible problem with the engine’s intercylinder baffles. These are small, odd-shaped pieces of aluminum that sit beneath and between adjacent pairs of cylinders and prevent cooling air from flowing through the gap between the cylinders and bypassing the cooling fins.
In the meantime, Wade had relocated from Wisconsin to Wyoming, where Cirrus-qualified maintenance shops are few and far between. So, when Wade reported having an issue with his Avidyne DFC100 autopilot, Jeff recommended that he take the airplane to Arapahoe Aero at Centennial Airport (APA) just south of Denver. Arapahoe is a Cirrus Authorized Service Center with a good avionics shop, and Savvy’s prior experience with Arapahoe had been excellent.
Jeff contacted Arapahoe’s director of maintenance, John Wells, and asked that he put Wade’s airplane on the avionics shop schedule for autopilot work. Jeff also told John that the airplane had been having a persistent problem with elevated number 3 CHT and asked if John would inspect the engine to see if he could find anything that might be responsible for this, with special emphasis on the intercylinder baffles. John said he’d be happy to have a look.
Wade flew the airplane to Centennial. The avionics shop worked on the autopilot while John and one of his most senior technicians inspected the airplane’s engine. A few days later, John sent Jeff the following message:
“We have been looking at the engine and I think we may have found the culprit. The intercylinder baffles on the right side of the engine are installed incorrectly. They are location-specific on the IO-550-N, and the baffles appear to be swapped front to back. This may seem like a minor thing, but we have seen it make a significant difference in the past. I would recommend swapping the baffles into their correct position and performing a test flight.”
Bingo! Once the right-hand front and rear intercylinder baffles were moved to their proper locations, the test flight showed that the number 3 CHT had returned to normal, and Wade’s two-year quest for a solution was finally over. Once again, this mistake didn’t happen at the Continental factory; it happened during cylinder work in the field. A perceptive diagnosis and a sharp set of eyes resolved another elusive maintenance-induced issue.